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When all was welded and cooled down I tightened the
25mm bolt as much as I could using a length of pipe for more leverage - no
movement was seen, then repeated heavy blows to the bolt head and more attempts
to screw the bolt I could see the existing key starting to pull through the
weld. cannot believe how tight it was in.
More welding above the key including a piece of round across the whole lot
was added and the above procedure was repeated - slog the bolt, turn the bolt,
sweat (as it was 36 deg C) and finally after much effort I could see slight
movement, the procedure continued until it came loose.
Other than careless grinding by myself where I touched the flywheel no
damage to shaft or flywheel occurs using this method and I doubt that I could
have got the key out using any other method and yes no prize for saying I am a
rough welder :-))
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